Painfull Heath! Painfull! So take me back again... you had already rebuilt this motor, and it went south on you during it's trials did it not? Was this a failure on your part, or a a machine shops boo boo? Everybody wants to know how to prevent this sort of thing.
The used oil analysis done before pulling the heads the 1st time showed a very small amount of coolant. The headgasket was starting to fail on the #1 cylinder (seen at the time the heads where pulled last year). The heads where gone through and reported as good. I put on a set of VR headgaskets, ARP studs, turbo, and put it back together. There were other issues (bad flywheel, injector failures, blah, blah, blah), but the headgasket let go within a few thousand miles as Scott said, on my way to the Rally in PA. It would only spew coolant when pulling the camper. It never got hot, until the last camping trip we took and I was dang close to home thank God. 


