Well first I checked it with playdough and the exhaust side was smashed so thin it was difficult to measure. The intake side was plenty (i don't remember exactly what it was, but it was quite a bit). So then I tried checking it with a dial indicator and could only get the exhaust valve to move ever so slightly somewhere between. 001-.003in. I tried retarding it and it made it worse to the point the valve would actually hit the piston. I didn't try to advance it, but it was a long day of on and off with the head and double and triple checking everything so I just went back to a stock cam.