Rossroams
Full Access Member
Hey everyone, so I recently put a H1C on my 6.9 IDI which I mated to the previous factory turbo kit. I hooked up a boost gauge and took it for a drive; sounded great but lacked even a 1 psi. So I take the turbo off and leave just the up pipe and ATS intake snail attached. Then I put my hand over the intake snail while it's running expecting it to sputter... nope, keeps running fine, even with my hand blocking the intake!!! Where else could it be drawing air in from, the CDR hole I poked holes in to drain oil? Or did the shop I payed to have this thing resealed stuff me. Any advice would help! Should I murder the mechanics who took 3&1/2 months to rebuild it?!